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 Post subject: Oops at Naugatuck with FL9
PostPosted: Sun Jun 29, 2025 8:28 pm 

Joined: Sun Aug 22, 2004 1:51 pm
Posts: 11879
Location: Somewhere east of Prescott, AZ along the old Santa Fe "Prescott & Eastern"
Apparently ex-New Haven FL9 2019 picked a switch during a photo charter at the Naugatuck RR today:

https://www.youtube.com/watch?v=CsVP0Sonj3c

The charter was for Railfan Day to "raise funds for the Mount Rainier Scenic Railroad historic wooden bridge rehabilitation that was tragically lost due to an arson fire." The RR Museum of New England was to split total gross revenue 50/50 with the non profit Mount Rainier Scenic Railroad.

UPDATE:
Previously linked video got set to "private"; here's another one:

https://www.youtube.com/watch?v=yRKYlhWPXfQ


Last edited by Alexander D. Mitchell IV on Sun Jun 29, 2025 9:49 pm, edited 1 time in total.

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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Sun Jun 29, 2025 8:48 pm 

Joined: Mon Dec 06, 2021 4:36 pm
Posts: 341
Yikes. And they just got the 2019 running again this spring after it was OoS for a couple years.


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Sun Jun 29, 2025 9:54 pm 

Joined: Mon Jan 17, 2005 9:06 pm
Posts: 2565
Location: Thomaston & White Plains
No one was injured. The incident is being investigated, and everything involved will be inspected. It occured during a low-speed photo runby.

Howard P.

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"I'm a railroad man, not a prophet."


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Mon Jun 30, 2025 11:15 am 

Joined: Tue Dec 06, 2022 8:31 am
Posts: 82
Hi
Just wondering how many people were still on the train( in the coaches) when it derailed???

Or were the coaches empty,, during the photo runby??

Also was the trip sold out,, hopefully everyone was safe during the derailment , those that were in the coaches, that did not do the low speed photo runby... Pat.


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Mon Jun 30, 2025 1:06 pm 
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Joined: Fri Oct 24, 2008 9:05 pm
Posts: 1094
Location: MA
Well that really sucks especially considering this was being done to help another Railroad. Remember hearing something about FL9's being hard on tracks because of their elongated three axle rear truck. Anyways that was fast acting on the crews part getting the train stop so fast after it went on the ground.


Last edited by RCD on Mon Jun 30, 2025 4:34 pm, edited 1 time in total.

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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Mon Jun 30, 2025 3:42 pm 

Joined: Sat May 11, 2024 12:44 pm
Posts: 1
While it wasn't an ideal situation, everyone handled it well, and the rest of the day was overall a success. Things happen on every railroad.


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Mon Jun 30, 2025 9:27 pm 

Joined: Mon Dec 06, 2021 4:36 pm
Posts: 341
RCD wrote:
Remember hearing something about FL9's being hard on tracks because of their elongated three axle rear truck.


Someone claimed that LIRR had similar issues with their Fairbanks-Morse CPA-24-5s.


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Thu Jul 03, 2025 3:16 pm 

Joined: Sun Oct 24, 2004 10:29 am
Posts: 364
Location: Scranton, PA
It could happen to anybody. I hope the damage isn't as bad as they think.


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Thu Jul 03, 2025 3:56 pm 

Joined: Thu Oct 24, 2019 11:05 pm
Posts: 188
In the real world of railroading - doo doo happens. Rerail, rinse and go on!


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Thu Jul 03, 2025 9:12 pm 

Joined: Sun Aug 22, 2004 9:54 am
Posts: 1040
Location: NJ
Just a bit of information. There were comments about the rear truck wheelbase on the FL-9 and that the LIRR had trouble with the F-M C-liners. That EMD truck has a 163 inch wheelbase, and is a normal 3 motor Flexicoil truck, minus the center motor, of course.

The A-1-A truck used by Alco, BLW and F-M on their passenger units had a wheelbase of 186 inches, almost two feet longer. I've never heard or read anything bad about how the PAs tracked or that they were rough on track.


Last edited by EDM on Sun Jul 06, 2025 12:22 pm, edited 1 time in total.

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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Thu Jul 03, 2025 9:12 pm 

Joined: Sun Aug 22, 2004 9:54 am
Posts: 1040
Location: NJ
Just a bit of information. There were comments about the rear truck wheelbase on the FL-9 and that the LIRR had trouble with the F-M C-liners. That EMD truck has a 163 inch wheelbase, and is a normal 3 motor Flexicoil truck, minus the center motor, of course.

The A-1-A truck used by Alco, BLW and F-M on their passenger units had a wheelbase of 186 inches, almost two feet longer. I've never heard or read anything bad about how the PAs tracked or that they were rough on track.


Last edited by EDM on Sun Jul 06, 2025 12:23 pm, edited 1 time in total.

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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Sat Jul 05, 2025 8:34 pm 

Joined: Wed Jan 17, 2018 8:48 pm
Posts: 7
Fellow did a walkaround video, provides much better detail of the aftermath:

https://youtu.be/TGTKP8Zg1PM?si=nz0e6zituIgHfH3f

Note the horn and numberboards are absent; removed for safekeeping or liberated by some lower element of the hobby?


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 Post subject: Re: Oops at Naugatuck with FL9
PostPosted: Sat Jul 05, 2025 9:01 pm 

Joined: Sun Aug 22, 2004 9:54 am
Posts: 1040
Location: NJ
I was on that trip and have been in touch with some of the Naugatuck people this week. The Hancock air whistle was removed by the shop manager Sunday afternoon. I'm not sure about the number boards, but I would assume they went into safekeeping as well, maybe on Monday or Tuesday. The locomotive was rerailed midweek, using a crane, and is back in the shop for evaluation and repairs. Some of the siding was removed to allow access for the crane.

I don't normally comment on things I see on YouTube, but I have to address the suggestion that the East Litchfield siding is unused and should be taken up. It is frequently used for storage of maintenance of way equipment; three pieces of MofW equipment were on that siding Sunday, in fact. It has also been used as a team track, for receiving oversized loads like transformers. I understand that the siding will be restored.


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